When a skb has multiple vlans and it is CHECKSUM_PARTIAL,
igbvf_tx_csum() fails to get the network protocol and checksum related
descriptor fields are not configured correctly because skb->protocol
doesn't show the L3 protocol in this case.
Use vlan_get_protocol() to get the proper network protocol.
Signed-off-by: Toshiaki Makita <makita.toshiaki@lab.ntt.co.jp>
Signed-off-by: David S. Miller <davem@davemloft.net>
A recent patch tried to work around a valid warning for the use of a
deprecated interface by blindly changing from the old
pcmcia_request_exclusive_irq() interface to pcmcia_request_irq().
This driver has an interrupt handler that is not currently aware
of shared interrupts, but can be easily converted to be.
At the moment, the driver reads the interrupt status register
repeatedly until it contains only zeroes in the interesting bits,
and handles each bit individually.
This patch adds the missing part of returning IRQ_NONE in case none
of the bits are set to start with, so we can move on to the next
interrupt source.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Fixes: 5f5316fcd0 ("am2150: Update nmclan_cs.c to use update PCMCIA API")
Signed-off-by: David S. Miller <davem@davemloft.net>
The ni65 and lance ethernet drivers manually program the ISA DMA
controller that is only available on x86 PCs and a few compatible
systems. Trying to build it on ARM results in this error:
ni65.c: In function 'ni65_probe1':
ni65.c:496:62: error: 'DMA1_STAT_REG' undeclared (first use in this function)
((inb(DMA1_STAT_REG) >> 4) & 0x0f)
^
ni65.c:496:62: note: each undeclared identifier is reported only once for each function it appears in
ni65.c:497:63: error: 'DMA2_STAT_REG' undeclared (first use in this function)
| (inb(DMA2_STAT_REG) & 0xf0);
The DMA1_STAT_REG and DMA2_STAT_REG registers are only defined for
alpha, mips, parisc, powerpc and x86, although it is not clear
which subarchitectures actually have them at the correct location.
This patch for now just disables it for ARM, to avoid randconfig
build errors. We could also decide to limit it to the set of
architectures on which it does compile, but that might look more
deliberate than guessing based on where the drivers build.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Signed-off-by: David S. Miller <davem@davemloft.net>
The cosa driver is rather outdated and does not get built on most
platforms because it requires the ISA_DMA_API symbol. However
there are some ARM platforms that have ISA_DMA_API but no virt_to_bus,
and they get this build error when enabling the ltpc driver.
drivers/net/wan/cosa.c: In function 'tx_interrupt':
drivers/net/wan/cosa.c:1768:3: error: implicit declaration of function 'virt_to_bus'
unsigned long addr = virt_to_bus(cosa->txbuf);
^
The same problem exists for the Hostess SV-11 and Sealevel Systems 4021
drivers.
This adds another dependency in Kconfig to avoid that configuration.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Signed-off-by: David S. Miller <davem@davemloft.net>
The cs89x0 driver can either be built as an ISA driver or a platform
driver, the choice is controlled by the CS89x0_PLATFORM Kconfig
symbol. Building the ISA driver on a system that does not have
a way to map I/O ports fails with this error:
drivers/built-in.o: In function `cs89x0_ioport_probe.constprop.1':
:(.init.text+0x4794): undefined reference to `ioport_map'
:(.init.text+0x4830): undefined reference to `ioport_unmap'
This changes the Kconfig logic to take that option away and
always force building the platform variant of this driver if
CONFIG_HAS_IOPORT_MAP is not set. This is the only correct
choice in this case, and it avoids the build error.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Signed-off-by: David S. Miller <davem@davemloft.net>
When we've run out of space in the output buffer to store more data, we
will call zlib_deflate with a NULL output buffer until we've consumed
remaining input.
When this happens, olen contains the size the output buffer would have
consumed iff we'd have had enough room.
This can later cause skb_over_panic when ppp_generic skb_put()s
the returned length.
Reported-by: Iain Douglas <centos@1n6.org.uk>
Signed-off-by: Florian Westphal <fw@strlen.de>
Signed-off-by: David S. Miller <davem@davemloft.net>
Rename the netns to src_net to avoid confusion with the netns where the
interface stands. The user may specify IFLA_NET_NS_[PID|FD] to create
a x-netns netndevice: IFLA_NET_NS_[PID|FD] points to the netns where the
netdevice stands and src_net to the link netns.
Note that before commit f01ec1c017 ("vxlan: add x-netns support"), it was
possible to create a x-netns vxlan netdevice, but the netdevice was not
operational.
Fixes: f01ec1c017 ("vxlan: add x-netns support")
Signed-off-by: Nicolas Dichtel <nicolas.dichtel@6wind.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
src_net points to the netns where the netlink message has been received. This
netns may be different from the netns where the interface is created (because
the user may add IFLA_NET_NS_[PID|FD]). In this case, src_net is the link netns.
It seems wrong to override the netns in the newlink() handler because if it
was not already src_net, it means that the user explicitly asks to create the
netdevice in another netns.
CC: Sjur Brændeland <sjur.brandeland@stericsson.com>
CC: Dmitry Tarnyagin <dmitry.tarnyagin@lockless.no>
Fixes: 8391c4aab1 ("caif: Bugfixes in CAIF netdevice for close and flow control")
Fixes: c412540063 ("caif-hsi: Add rtnl support")
Signed-off-by: Nicolas Dichtel <nicolas.dichtel@6wind.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
In the case when alloc_netdev fails we return NULL to a caller. But there is no
check for NULL in the probe drivers. This patch changes NULL to an error
pointer. The function description is amended to reflect what we may get
returned.
Signed-off-by: Andy Shevchenko <andriy.shevchenko@linux.intel.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
With the commit d75b1ade56 ("net: less interrupt masking in NAPI") napi
repoll is done only when work_done == budget. When in busy_poll is we return 0
in napi_poll. We should return budget.
Signed-off-by: Govindarajulu Varadarajan <_govind@gmx.com>
Acked-by: Eric Dumazet <edumazet@google.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
- Use the return value of dma_map_single(), rather than calling
virt_to_page() separately
- Check for mapping failue
- Call dma_unmap_single() rather than dma_sync_single_for_cpu()
Signed-off-by: Ben Hutchings <ben.hutchings@codethink.co.uk>
Signed-off-by: David S. Miller <davem@davemloft.net>
dma_map_single() may fail if an IOMMU or swiotlb is in use, so
we need to check for this.
Signed-off-by: Ben Hutchings <ben.hutchings@codethink.co.uk>
Signed-off-by: David S. Miller <davem@davemloft.net>
Currently we try to clear EDRRR and EDTRR and immediately continue to
free buffers. This is unsafe because:
- In general, register writes are not serialised with DMA, so we still
have to wait for DMA to complete somehow
- The R8A7790 (R-Car H2) manual states that the TX running flag cannot
be cleared by writing to EDTRR
- The same manual states that clearing the RX running flag only stops
RX DMA at the next packet boundary
I applied this patch to the driver to detect DMA writes to freed
buffers:
> --- a/drivers/net/ethernet/renesas/sh_eth.c
> +++ b/drivers/net/ethernet/renesas/sh_eth.c
> @@ -1098,7 +1098,14 @@ static void sh_eth_ring_free(struct net_device *ndev)
> /* Free Rx skb ringbuffer */
> if (mdp->rx_skbuff) {
> for (i = 0; i < mdp->num_rx_ring; i++)
> + memcpy(mdp->rx_skbuff[i]->data,
> + "Hello, world", 12);
> + msleep(100);
> + for (i = 0; i < mdp->num_rx_ring; i++) {
> + WARN_ON(memcmp(mdp->rx_skbuff[i]->data,
> + "Hello, world", 12));
> dev_kfree_skb(mdp->rx_skbuff[i]);
> + }
> }
> kfree(mdp->rx_skbuff);
> mdp->rx_skbuff = NULL;
then ran the loop:
while ethtool -G eth0 rx 128 ; ethtool -G eth0 rx 64; do echo -n .; done
and 'ping -f' toward the sh_eth port from another machine. The
warning fired several times a minute.
To fix these issues:
- Deactivate all TX descriptors rather than writing to EDTRR
- As there seems to be no way of telling when RX DMA is stopped,
perform a soft reset to ensure that both DMA enginess are stopped
- To reduce the possibility of the reset truncating a transmitted
frame, disable egress and wait a reasonable time to reach a
packet boundary before resetting
- Update statistics before resetting
(The 'reasonable time' does not allow for CS/CD in half-duplex
mode, but half-duplex no longer seems reasonable!)
Signed-off-by: Ben Hutchings <ben.hutchings@codethink.co.uk>
Signed-off-by: David S. Miller <davem@davemloft.net>
If RX traffic is overflowing the FIFO or DMA ring, logging every time
this happens just makes things worse. These errors are visible in the
statistics anyway.
Signed-off-by: Ben Hutchings <ben.hutchings@codethink.co.uk>
Signed-off-by: David S. Miller <davem@davemloft.net>
While being in an ERROR_WARNING state, and receiving further
bus error events with error counters still in the ERROR_WARNING
range of 97-127 inclusive, the state handling code erroneously
reverts back to ERROR_ACTIVE.
Per the CAN standard, only revert to ERROR_ACTIVE when the
error counters are less than 96.
Moreover, in certain Kvaser models, the BUS_ERROR flag is
always set along with undefined bits in the M16C status
register. Thus use bitwise operators instead of full equality
for checking that register against bus errors.
Signed-off-by: Ahmed S. Darwish <ahmed.darwish@valeo.com>
Cc: linux-stable <stable@vger.kernel.org>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
On some x86 laptops, plugging a Kvaser device again after an
unplug makes the firmware always ignore the very first command.
For such a case, provide some room for retries instead of
completely exiting the driver init code.
Signed-off-by: Ahmed S. Darwish <ahmed.darwish@valeo.com>
Cc: linux-stable <stable@vger.kernel.org>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Send expected argument to the URB completion hander: a CAN
netdevice instead of the network interface private context
`kvaser_usb_net_priv'.
This was discovered by having some garbage in the kernel
log in place of the netdevice names: can0 and can1.
Signed-off-by: Ahmed S. Darwish <ahmed.darwish@valeo.com>
Cc: linux-stable <stable@vger.kernel.org>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Upon receiving a hardware event with the BUS_RESET flag set,
the driver kills all of its anchored URBs and resets all of
its transmit URB contexts.
Unfortunately it does so under the context of URB completion
handler `kvaser_usb_read_bulk_callback()', which is often
called in an atomic context.
While the device is flooded with many received error packets,
usb_kill_urb() typically sleeps/reschedules till the transfer
request of each killed URB in question completes, leading to
the sleep in atomic bug. [3]
In v2 submission of the original driver patch [1], it was
stated that the URBs kill and tx contexts reset was needed
since we don't receive any tx acknowledgments later and thus
such resources will be locked down forever. Fortunately this
is no longer needed since an earlier bugfix in this patch
series is now applied: all tx URB contexts are reset upon CAN
channel close. [2]
Moreover, a BUS_RESET is now treated _exactly_ like a BUS_OFF
event, which is the recommended handling method advised by
the device manufacturer.
[1] http://article.gmane.org/gmane.linux.network/239442http://www.webcitation.org/6Vr2yagAQ
[2] can: kvaser_usb: Reset all URB tx contexts upon channel close
889b77f7fd
[3] Stacktrace:
<IRQ> [<ffffffff8158de87>] dump_stack+0x45/0x57
[<ffffffff8158b60c>] __schedule_bug+0x41/0x4f
[<ffffffff815904b1>] __schedule+0x5f1/0x700
[<ffffffff8159360a>] ? _raw_spin_unlock_irqrestore+0xa/0x10
[<ffffffff81590684>] schedule+0x24/0x70
[<ffffffff8147d0a5>] usb_kill_urb+0x65/0xa0
[<ffffffff81077970>] ? prepare_to_wait_event+0x110/0x110
[<ffffffff8147d7d8>] usb_kill_anchored_urbs+0x48/0x80
[<ffffffffa01f4028>] kvaser_usb_unlink_tx_urbs+0x18/0x50 [kvaser_usb]
[<ffffffffa01f45d0>] kvaser_usb_rx_error+0xc0/0x400 [kvaser_usb]
[<ffffffff8108b14a>] ? vprintk_default+0x1a/0x20
[<ffffffffa01f5241>] kvaser_usb_read_bulk_callback+0x4c1/0x5f0 [kvaser_usb]
[<ffffffff8147a73e>] __usb_hcd_giveback_urb+0x5e/0xc0
[<ffffffff8147a8a1>] usb_hcd_giveback_urb+0x41/0x110
[<ffffffffa0008748>] finish_urb+0x98/0x180 [ohci_hcd]
[<ffffffff810cd1a7>] ? acct_account_cputime+0x17/0x20
[<ffffffff81069f65>] ? local_clock+0x15/0x30
[<ffffffffa000a36b>] ohci_work+0x1fb/0x5a0 [ohci_hcd]
[<ffffffff814fbb31>] ? process_backlog+0xb1/0x130
[<ffffffffa000cd5b>] ohci_irq+0xeb/0x270 [ohci_hcd]
[<ffffffff81479fc1>] usb_hcd_irq+0x21/0x30
[<ffffffff8108bfd3>] handle_irq_event_percpu+0x43/0x120
[<ffffffff8108c0ed>] handle_irq_event+0x3d/0x60
[<ffffffff8108ec84>] handle_fasteoi_irq+0x74/0x110
[<ffffffff81004dfd>] handle_irq+0x1d/0x30
[<ffffffff81004727>] do_IRQ+0x57/0x100
[<ffffffff8159482a>] common_interrupt+0x6a/0x6a
Signed-off-by: Ahmed S. Darwish <ahmed.darwish@valeo.com>
Cc: linux-stable <stable@vger.kernel.org>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Commit 69ad0dd7af
Author: Ezequiel Garcia <ezequiel.garcia@free-electrons.com>
Date: Mon May 19 13:59:59 2014 -0300
net: mv643xx_eth: Use dma_map_single() to map the skb fragments
caused a nasty regression by removing the support for highmem skb
fragments. By using page_address() to get the address of a fragment's
page, we are assuming a lowmem page. However, such assumption is incorrect,
as fragments can be in highmem pages, resulting in very nasty issues.
This commit fixes this by using the skb_frag_dma_map() helper,
which takes care of mapping the skb fragment properly. Additionally,
the type of mapping is now tracked, so it can be unmapped using
dma_unmap_page or dma_unmap_single when appropriate.
This commit also fixes the error path in txq_init() to release the
resources properly.
Fixes: 69ad0dd7af ("net: mv643xx_eth: Use dma_map_single() to map the skb fragments")
Reported-by: Russell King <rmk+kernel@arm.linux.org.uk>
Signed-off-by: Ezequiel Garcia <ezequiel.garcia@free-electrons.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
In order to stop the RX path accessing the RX ring while it's being
stopped or resized, we clear the interrupt mask (EESIPR) and then call
free_irq() or synchronise_irq(). This is insufficient because the
interrupt handler or NAPI poller may set EESIPR again after we clear
it. Also, in sh_eth_set_ringparam() we currently don't disable NAPI
polling at all.
I could easily trigger a crash by running the loop:
while ethtool -G eth0 rx 128 && ethtool -G eth0 rx 64; do echo -n .; done
and 'ping -f' toward the sh_eth port from another machine.
To fix this:
- Add a software flag (irq_enabled) to signal whether interrupts
should be enabled
- In the interrupt handler, if the flag is clear then clear EESIPR
and return
- In the NAPI poller, if the flag is clear then don't set EESIPR
- Set the flag before enabling interrupts in sh_eth_dev_init() and
sh_eth_set_ringparam()
- Clear the flag and serialise with the interrupt and NAPI
handlers before clearing EESIPR in sh_eth_close() and
sh_eth_set_ringparam()
After this, I could run the loop for 100,000 iterations successfully.
Signed-off-by: Ben Hutchings <ben.hutchings@codethink.co.uk>
Signed-off-by: David S. Miller <davem@davemloft.net>
If the device is down then no packet buffers should be allocated.
We also must not touch its registers as it may be powered off.
Signed-off-by: Ben Hutchings <ben.hutchings@codethink.co.uk>
Signed-off-by: David S. Miller <davem@davemloft.net>
We must only ever stop TX queues when they are full or the net device
is not 'ready' so far as the net core, and specifically the watchdog,
is concerned. Otherwise, the watchdog may fire *immediately* if no
packets have been added to the queue in the last 5 seconds.
What's more, sh_eth_tx_timeout() will likely crash if called while
we're resizing the TX ring.
I could easily trigger this by running the loop:
while ethtool -G eth0 rx 128 && ethtool -G eth0 rx 64; do echo -n .; done
Signed-off-by: Ben Hutchings <ben.hutchings@codethink.co.uk>
Signed-off-by: David S. Miller <davem@davemloft.net>
If an skb to be transmitted is shorter than the minimum Ethernet frame
length, we currently set the DMA descriptor length to the minimum but
do not add zero-padding. This could result in leaking sensitive
data. We also pass different lengths to dma_map_single() and
dma_unmap_single().
Use skb_padto() to pad properly, before calling dma_map_single().
Signed-off-by: Ben Hutchings <ben.hutchings@codethink.co.uk>
Signed-off-by: David S. Miller <davem@davemloft.net>
In Dual EMAC, the default VLANs are used to segregate Rx packets between
the ports, so adding the same default VLAN to the switch will affect the
normal packet transfers. So returning error on addition of dual EMAC
default VLANs.
Even if EMAC 0 default port VLAN is added to EMAC 1, it will lead to
break dual EMAC port separations.
Fixes: d9ba8f9e62 (driver: net: ethernet: cpsw: dual emac interface implementation)
Cc: <stable@vger.kernel.org> # v3.9+
Reported-by: Felipe Balbi <balbi@ti.com>
Signed-off-by: Mugunthan V N <mugunthanvnm@ti.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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Merge tag 'linux-can-fixes-for-3.19-20150121' of git://git.kernel.org/pub/scm/linux/kernel/git/mkl/linux-can
Marc Kleine-Budde says:
====================
pull-request: can 2015-01-21
this is a pull request for v3.19, net/master, which consists of a single patch.
Viktor Babrian fixes the issue in the c_can dirver, that the CAN interface
might continue to send frames after the interface has been shut down.
====================
Signed-off-by: David S. Miller <davem@davemloft.net>
The ip6_route_output() always returns a valid dst pointer unlike in IPv4
case. So the validation has to be different from the IPv4 path. Correcting
that error in this patch.
This was picked up by a static checker with a following warning -
drivers/net/ipvlan/ipvlan_core.c:380 ipvlan_process_v6_outbound()
warn: 'dst' isn't an ERR_PTR
Signed-off-by: Mahesh Bandewar <maheshb@google.com>
Reported-by: Dan Carpenter <dan.carpenter@oracle.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
NAPI poll logic now enforces that a poller returns exactly the budget
when it wants to be called again.
If a driver limits TX completion, it has to return budget as well when
the limit is hit, not the number of received packets.
Reported-and-tested-by: Mike Galbraith <umgwanakikbuti@gmail.com>
Signed-off-by: Eric Dumazet <edumazet@google.com>
Fixes: d75b1ade56 ("net: less interrupt masking in NAPI")
Cc: Manish Chopra <manish.chopra@qlogic.com>
Acked-by: Manish Chopra <manish.chopra@qlogic.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
With the commit d75b1ade56 ("net: less interrupt masking in NAPI") napi repoll
is done only when work_done == budget. When we are in busy_poll we return 0 in
napi_poll. We should return budget.
Signed-off-by: Govindarajulu Varadarajan <_govind@gmx.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
* fix an IRQ storm caused by commit 872b5d814f
iwlwifi:
* A fix for scan that fixes a firmware assertion
* A fix that improves roaming behavior. Same fix has been tested for
a while in iwldvm. This is a bit of a work around, but the real fix
should be in mac80211 and will come later.
* A fix for BARs that avoids a WARNING.
* one fix for rfkill while scheduled scan is running.
Linus's system hit this issue. WiFi would be unavailable
after this has happpened because of bad state in cfg80211.
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Merge tag 'wireless-drivers-for-davem-2015-01-20' of git://git.kernel.org/pub/scm/linux/kernel/git/kvalo/wireless-drivers
ath9k:
* fix an IRQ storm caused by commit 872b5d814f
iwlwifi:
* A fix for scan that fixes a firmware assertion
* A fix that improves roaming behavior. Same fix has been tested for
a while in iwldvm. This is a bit of a work around, but the real fix
should be in mac80211 and will come later.
* A fix for BARs that avoids a WARNING.
* one fix for rfkill while scheduled scan is running.
Linus's system hit this issue. WiFi would be unavailable
after this has happpened because of bad state in cfg80211.
Signed-off-by: David S. Miller <davem@davemloft.net>
Updated hardware documention shows the Rx flow control settings were
moved from the Rx queue operation mode register to a new Rx queue flow
control register. The old flow control settings are now reserved areas
of the Rx queue operation mode register. Update the code to use the new
register.
Signed-off-by: Tom Lendacky <thomas.lendacky@amd.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Put controller into init mode in network stop to end pending transmissions. The
issue is observed in cases when transmitted frame is not acked.
Signed-off-by: Viktor Babrian <babrian.viktor@renyi.mta.hu>
Cc: linux-stable <stable@vger.kernel.org>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
"sp->desc[i]" has 25 characters. "dev->name" has 15 characters. If we
used all 15 characters then the sprintf() would overflow.
I changed the "sprintf(sp->name, "%s Neterion %s"" to snprintf(), as
well, even though it can't overflow just to be consistent.
Signed-off-by: Dan Carpenter <dan.carpenter@oracle.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Read OCP register 0xa43a~0xa43b would clear some flags which the hw
would use, and it may let the device lost. However, the unit of
reading is 4 bytes. That is, it would read 0xa438~0xa43b when calling
sram_read() to read OCP_SRAM_DATA.
Signed-off-by: Hayes Wang <hayeswang@realtek.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
For ocp_write_word() and ocp_write_byte(), there is a generic_ocp_read()
which is used to read the whole 4 byte data, keep the unchanged bytes,
and modify the expected bytes. However, the "byen" could be used to
determine which bytes of the 4 bytes to write, so the action could be
removed.
Signed-off-by: Hayes Wang <hayeswang@realtek.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
IRQs should only get activated when there is nothing to poll in the
queue any more and to after every poll.
Signed-off-by: Hauke Mehrtens <hauke@hauke-m.de>
Signed-off-by: David S. Miller <davem@davemloft.net>
napi should get registered before the netdev and not after.
Signed-off-by: Hauke Mehrtens <hauke@hauke-m.de>
Signed-off-by: David S. Miller <davem@davemloft.net>
The driver connects and disconnects the PHY device whenever the
net device is brought up and down. The ethtool get_settings,
set_settings and nway_reset operations will dereference a null
or dangling pointer if called while it is down.
I think it would be preferable to keep the PHY connected, but there
may be good reasons not to.
As an immediate fix for this bug:
- Set the phydev pointer to NULL after disconnecting the PHY
- Change those three operations to return -ENODEV while the PHY is
not connected
Signed-off-by: Ben Hutchings <ben.hutchings@codethink.co.uk>
Signed-off-by: David S. Miller <davem@davemloft.net>
Currently net_device_ops::set_rx_mode is only implemented for
chips with a TSU (multiple address table). However we do need
to turn the PRM (promiscuous) flag on and off for other chips.
- Remove the unlikely() from the TSU functions that we may safely
call for chips without a TSU
- Make setting of the MCT flag conditional on the tsu capability flag
- Rename sh_eth_set_multicast_list() to sh_eth_set_rx_mode() and plumb
it into both net_device_ops structures
- Remove the previously-unreachable branch in sh_eth_rx_mode() that
would otherwise reset the flags to defaults for non-TSU chips
Signed-off-by: Ben Hutchings <ben.hutchings@codethink.co.uk>
Signed-off-by: David S. Miller <davem@davemloft.net>
To fix invalid hardware accesses, the commit 872b5d814f ("ath9k: do not
access hardware on IRQs during reset") made the irq handler ignore interrupts
emitted after queueing a hardware reset (which disables the IRQ). This left a
small time window for the IRQ to get re-enabled by the tasklet, which caused
IRQ storms. Instead of returning IRQ_NONE when ATH_OP_HW_RESET is set, disable
the IRQ entirely for the duration of the reset.
Signed-off-by: Felix Fietkau <nbd@openwrt.org>
Signed-off-by: Kalle Valo <kvalo@codeaurora.org>
Linus's system hit this issue. WiFi would be unavailable
after this has happpened because of bad state in cfg80211.
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Merge tag 'iwlwifi-for-kalle-2015-01-15' of https://git.kernel.org/pub/scm/linux/kernel/git/iwlwifi/iwlwifi-fixes
* one fix for rfkill while scheduled scan is running.
Linus's system hit this issue. WiFi would be unavailable
after this has happpened because of bad state in cfg80211.
When we have an active scheduled scan, and the RFKILL
interrupt kicks in, the stack will cancel the scheduled
scan as part of the down flow. But cancelling scheduled
scan usually implies sending a command to the firwmare
which has been killed as part of the RFKILL interrupt
handling.
Because of that, we returned an error to mac80211 when
it asked to stop the scheduled scan and didn't notify the
end of the scheduled scan. Besides a fat warning, this led
to a situation in which cfg80211 would refuse any new scan
request.
To disentangle this, fake that the scheduled scan has been
stopped without sending the command to the firwmare, return
0 after having properly let cfg80211 know that the scan
has been cancelled.
This is basically the same as:
commit 9b520d8495
Author: Emmanuel Grumbach <emmanuel.grumbach@intel.com>
Date: Tue Nov 4 15:54:11 2014 +0200
iwlwifi: mvm: abort scan upon RFKILL
This code existed but not for all the different FW APIs
we support.
Fix this.
but for the scheduled scan case.
Link: http://permalink.gmane.org/gmane.linux.kernel.wireless.general/133232
Reported-by: Linus Torvalds <torvalds@linux-foundation.org>
Signed-off-by: Emmanuel Grumbach <emmanuel.grumbach@intel.com>
On dm816x we have two emac controllers with separate memory
areas.
Cc: Brian Hutchinson <b.hutchman@gmail.com>
Cc: Felipe Balbi <balbi@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Some devices like dm816x have the MDIO registers within the first EMAC
instance address space. Let's fix the issue by allowing to pass an
optional second IO range for the EMAC control register area.
Cc: Brian Hutchinson <b.hutchman@gmail.com>
Cc: Felipe Balbi <balbi@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Looks like the phy_id is never set up beyond getting the phandle.
Note that we can remove the ifdef for phy_node as there is a stub
for of_phy_connec() if CONFIG_OF is not set.
Cc: Brian Hutchinson <b.hutchman@gmail.com>
Cc: Felipe Balbi <balbi@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
We only use clk_get() to get the frequency, the rest is done by
the runtime PM calls. Let's free the clock too.
Cc: Brian Hutchinson <b.hutchman@gmail.com>
Cc: Felipe Balbi <balbi@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Commit 3ba9738134 ("net: ethernet: davinci_emac: add pm_runtime support")
added support for runtime PM, but it causes issues on omap3 related devices
that actually gate the clocks:
Unhandled fault: external abort on non-linefetch (0x1008)
...
[<c04160f0>] (emac_dev_getnetstats) from [<c04d6a3c>] (dev_get_stats+0x78/0xc8)
[<c04d6a3c>] (dev_get_stats) from [<c04e9ccc>] (rtnl_fill_ifinfo+0x3b8/0x938)
[<c04e9ccc>] (rtnl_fill_ifinfo) from [<c04eade4>] (rtmsg_ifinfo+0x68/0xd8)
[<c04eade4>] (rtmsg_ifinfo) from [<c04dd35c>] (register_netdevice+0x3a0/0x4ec)
[<c04dd35c>] (register_netdevice) from [<c04dd4bc>] (register_netdev+0x14/0x24)
[<c04dd4bc>] (register_netdev) from [<c041755c>] (davinci_emac_probe+0x408/0x5c8)
[<c041755c>] (davinci_emac_probe) from [<c0396d78>] (platform_drv_probe+0x48/0xa4)
Let's fix it by moving the pm_runtime_get() call earlier, and also add it to
the emac_dev_getnetstats(). Also note that we want to use pm_runtime_get_sync()
as we don't want to have deferred_resume happen. And let's also check the
return value for pm_runtime_get_sync() as noted by Felipe Balbi <balbi@ti.com>.
Cc: Brian Hutchinson <b.hutchman@gmail.com>
Acked-by: Mark A. Greer <mgreer@animalcreek.com>
Reviewed-by: Felipe Balbi <balbi@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
On davinci_emac, we have pulse interrupts. This means that we need to
clear the EOI bits when disabling interrupts as otherwise the interrupts
keep happening. And we also need to not clear the EOI bits again when
enabling the interrupts as otherwise we will get tons of:
unexpected IRQ trap at vector 00
These errors almost certainly mean that the omap-intc.c is signaling
a spurious interrupt with the reserved irq 127 as we've seen earlier
on omap3.
Let's fix the issue by clearing the EOI bits when disabling the
interrupts. Let's also keep the comment for "Rx Threshold and Misc
interrupts are not enabled" for both enable and disable so people
are aware of this when potentially adding more support.
Note that eventually we should handle the RX and TX interrupts
separately like cpsw is now doing. However, so far I have not seen
any issues with this based on my testing, so it seems to behave a
little different compared to the cpsw that had a similar issue.
Cc: Brian Hutchinson <b.hutchman@gmail.com>
Reviewed-by: Felipe Balbi <balbi@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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Merge tag 'linux-can-fixes-for-3.19-20150115' of git://git.kernel.org/pub/scm/linux/kernel/git/mkl/linux-can
Marc Kleine-Budde says:
====================
pull-request: can 2015-01-15
this is a pull request of 8 patches.
Ahmed S. Darwish contributes 4 fixes for the kvaser_usb driver. The two patches
by Oliver Hartkopp mark the m_can driver as non-ISO, as the CANFD standard was
updated. Roger Quadros's patch for the c_can driver fixes the register access
during RAMINIT. And one patch by my, which updates the MAINTAINERS file, as we
moved the git repos to the kernel.org infrastructure.
====================
Signed-off-by: David S. Miller <davem@davemloft.net>
Except for VXLAN steering rules, all offloads should work as they were
under plain DMFS mode. Fix that by enabling all the offloads under
DMFS-A0 mode, except for VXLAN steering rules.
Fixes: d57febe1a4 "net/mlx4: Add A0 hybrid steering"
Signed-off-by: Or Gerlitz <ogerlitz@mellanox.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
This patch fixes double kfree() calls at init_rx_ring() because
it causes static checker warning.
Reported-by: Dan Carpenter <dan.carpenter@oracle.com>
Signed-off-by: Byungho An <bh74.an@samsung.com>
Signed-off-by: Kukjin Kim <kgene@kernel.org>
Signed-off-by: David S. Miller <davem@davemloft.net>