forked from Minki/linux
arm64: Avoid clobbering mm in erratum workaround on QDF2400
Commit38fd94b027
("arm64: Work around Falkor erratum 1003") tried to work around a hardware erratum, but actually caused a system crash of its own during switch_mm: cpu_do_switch_mm+0x20/0x40 efi_virtmap_load+0x34/0x40 virt_efi_get_next_variable+0x64/0xc8 efivar_init+0x8c/0x348 efisubsys_init+0xd4/0x270 do_one_initcall+0x80/0x110 kernel_init_freeable+0x19c/0x240 kernel_init+0x10/0x100 ret_from_fork+0x10/0x50 Kernel panic - not syncing: Attempted to kill init! exitcode=0x0000000b In cpu_do_switch_mm, x1 contains the mm_struct pointer, which needs to be preserved by the pre_ttbr0_update_workaround macro rather than passed as a temporary. This patch clobbers x2 and x3 instead, keeping the mm_struct intact after the workaround has run. Fixes:38fd94b027
("arm64: Work around Falkor erratum 1003") Tested-by: Manoj Iyer <manoj.iyer@canonical.com> Signed-off-by: Shanker Donthineni <shankerd@codeaurora.org> Signed-off-by: Will Deacon <will.deacon@arm.com>
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@ -138,7 +138,7 @@ ENDPROC(cpu_do_resume)
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* - pgd_phys - physical address of new TTB
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*/
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ENTRY(cpu_do_switch_mm)
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pre_ttbr0_update_workaround x0, x1, x2
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pre_ttbr0_update_workaround x0, x2, x3
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mmid x1, x1 // get mm->context.id
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bfi x0, x1, #48, #16 // set the ASID
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msr ttbr0_el1, x0 // set TTBR0
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