slimbus: qcom-ngd-ctrl: Reduce auto suspend delay

Currently we have auto suspend delay of 1s which is
very high and it takes long time to driver for runtime
suspend after use case is done.

Hence to optimize runtime PM ops, reduce auto suspend
delay to 100ms.

Signed-off-by: Viken Dadhaniya <quic_vdadhani@quicinc.com>
Acked-by: Konrad Dybcio <konrad.dybcio@linaro.org>
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Link: https://lore.kernel.org/r/20240430091657.35428-2-srinivas.kandagatla@linaro.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This commit is contained in:
Viken Dadhaniya 2024-04-30 10:16:55 +01:00 committed by Greg Kroah-Hartman
parent 2a1ad6b752
commit 4286dbcecc

View File

@ -81,7 +81,6 @@
#define SLIM_USR_MC_DISCONNECT_PORT 0x2E
#define SLIM_USR_MC_REPEAT_CHANGE_VALUE 0x0
#define QCOM_SLIM_NGD_AUTOSUSPEND MSEC_PER_SEC
#define SLIM_RX_MSGQ_TIMEOUT_VAL 0x10000
#define SLIM_LA_MGR 0xFF
@ -1571,7 +1570,7 @@ static int qcom_slim_ngd_probe(struct platform_device *pdev)
platform_set_drvdata(pdev, ctrl);
pm_runtime_use_autosuspend(dev);
pm_runtime_set_autosuspend_delay(dev, QCOM_SLIM_NGD_AUTOSUSPEND);
pm_runtime_set_autosuspend_delay(dev, 100);
pm_runtime_set_suspended(dev);
pm_runtime_enable(dev);
pm_runtime_get_noresume(dev);